Skip to content
Snippets Groups Projects
final-project.md 23.5 KiB
Newer Older
Fabcloud's avatar
Fabcloud committed
# Final Project


Dan Stone's avatar
Dan Stone committed
My project will be a **vegetable washing machine** 
Fabcloud's avatar
Fabcloud committed

## Research

Dan Stone's avatar
Dan Stone committed
Goal is to create a  kitchen appliance that can wash and dry greens and 
other vegetables via a pre set cycle both saving time (and potentially water)

## Project description 

![VMS SKETCH](../images/imagW1/VMS06.jpeg){: style="height:360px;width:720px"}

![Veg Washing Machine](../images/Finalproject/VWMSKETCHV1.jpg){: style="height:300px;width:300px"}


Here is a first cut at the base:

![Base](../images/Finalproject/2basesetup.jpg)

**There are 4 main parts to the appliance**

1. Water reservoir 

2. Main container (Wash basin)- base is designed to have a gravity fed drain

3. Lid with build in sprinkler 

4. Vegetable holding bowel that sites in the Wash basin and spins to dry 

**There are 2 Motor/pump used**

1. Water pump to move water from reservoir to sprinkler head 

2. Motor to spin Vegetable bowel 

**There are 2 potential sensors**

1. Lid sensor - stop operation if lid is open mid cycle 

2. Water level sensor to alert if reservoir is empty 

**Microcontroller usage**

1. Control sequencing of pumps / motors 

2. Interrupt operation if sensor is triggered 

3. Manage GUI 

**GUI**

1. Based display and buttons

2. Allow user to start cycle 

- Wash only

- Dry only

- Wash/dry

3. Announce alerts (ready/water empty/finished)


Here is a another view of the merging design 

![Bottom](../images/Finalproject/2baseupview.jpg)



## Align parts to Fab Academy weekly topics  


 
| Weekly topics      | Parts |
| ----------- | ----------- |
| Computer controlled cutting | Outbox / wash basin holder  |
| Electronics production | Controller, motor ESC, Sensors  |
| 3D Scanning and printing | Motor housing, water connectors, sprinkler head, sproket/chain for motor drive|
| Electronics design | sensors / controller board / Motor ESC |
| Computer controlled machining |   Controller board  |
| Embedded programming | Cycle design / User input |
| Molding and casting | Drain / Spinning plate  |
| Input devices | GUI buttons / Sensors |
| Output devices | Screen |
 


Key component breakdown 

Outer box - Plexiglass  

Wash basin holder - Plexiglass / 3d print 

Water reservoir - molding / buying 

Electronic housing - 3D print 

spinner mechanism - 3D print 

Bowel - Molding / casting 

Lid - 3D Print 

Water pump / sprinkler mechanism - 3D print / electronics 

Sensors - 1) Lid sensor 2) Water level sensor 

Controller board -

Display/Buttons 

Water connections - 3 Print or buy 
Fabcloud's avatar
Fabcloud committed


## 2D and 3D Modeling

Dan Stone's avatar
Dan Stone committed
First I set up some user parameters I will use in sizing the spinning plate and it base 
Dan Stone's avatar
Dan Stone committed
![User Parameters](../images/ImagW2/GraphicApps/40platebase1.jpg)
Dan Stone's avatar
Dan Stone committed
Now I made a round leg for the plate to sit on 
Dan Stone's avatar
Dan Stone committed
![Leg sketch](../images/ImagW2/GraphicApps/40platebase2.jpg)
Dan Stone's avatar
Dan Stone committed
To create the shape of the base I will create a new sketch on the top of the base leg. I then
create a circle and replicate it using the circular pattern tool followed but a cut.
Dan Stone's avatar
Dan Stone committed
![Pattern](../images/ImagW2/GraphicApps/40platebase3.jpg)
Dan Stone's avatar
Dan Stone committed
![Cut](../images/ImagW2/GraphicApps/40platebase4.jpg)
Dan Stone's avatar
Dan Stone committed
I then sketched on top again and created a circle to create the plate itself 
Dan Stone's avatar
Dan Stone committed
![Plate](../images/ImagW2/GraphicApps/40platebase5.jpg)
Dan Stone's avatar
Dan Stone committed
Here I made a mistake as I did not select the whole plate and where the handy timeline 
tool come into play
Dan Stone's avatar
Dan Stone committed
![Plate](../images/ImagW2/GraphicApps/40platebase6correction.jpg)
Dan Stone's avatar
Dan Stone committed
And we are back on track. I wanted to create a downward facing lip in order to provide some water 
protection for the spinning mechanism during the dry cycle.
Dan Stone's avatar
Dan Stone committed
To do this I am going to draw a sketch of the lip and have it rotate around the plate center axis

Start with sketch

![Plate lip](../images/ImagW2/GraphicApps/40platebase7lip.jpg)

Then used the revolve to create the lip and set it to join the plate base.

![Plate lip](../images/ImagW2/GraphicApps/40platebase8revolve.jpg)

and there you go a first cut at the base plate 

![Plate](../images/ImagW2/GraphicApps/40platebase9.jpg)


Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
p4  
Dan Stone committed
## 3D printing the plate
Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
p4  
Dan Stone committed
I started off by printing a test model aprox 50 of the size 
Dan Stone's avatar
p4  
Dan Stone committed
![](../projects/Plate/Plate1.jpg)

After 5 hours, here it is:

When I put it up to the salad spinner bowel I have it seemed to me that the overall size of the machine \
can be much smaller then I originaly planned. 

Dan Stone's avatar
Dan Stone committed
I think a good approach is the max the size of the plate I can print on the MK3S
Dan Stone's avatar
p4  
Dan Stone committed

![](../projects/Plate/mk3s.jpg)

The original size had a 320mm diameter but I am going to resize it to a 200mm diameter 

![](../projects/Plate/Plate1.jpg)

I used the scale command leaving the Z as is and scaling the X and Y to 62.5% of the original 

Dan Stone's avatar
Dan Stone committed
Here it is printed
Dan Stone's avatar
p4  
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
![](../projects/Plate/Plate0.jpg)
Dan Stone's avatar
p4  
Dan Stone committed

Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
Now that I liked that size in order to make every thing work in fusion I had to go back and resize the plate in fusion to match.
Dan Stone's avatar
Dan Stone committed

![](../projects/Plate/Resize1.jpg)

![](../projects/Plate/Resize2.jpg)

Now we are ready to create the bowel holders
Dan Stone's avatar
p4  
Dan Stone committed

Dan Stone's avatar
Dan Stone committed

## Out runner motor mounting 

See below for discussion on the motor drive selection and decision to move to a direct drive mount on a outrunner motor. I am used a D3548.

![](../images/Finalproject/d3548.jpg)

I found a model of the motor I am planning to use on GrabCad 

![](../projects/Plate/Motor1.jpg)

This an out runner and I would like to cut its shape into the bottom of the spinner to test a direct drive

As the CAD was made of many many pieces it was easier to create a similar shaped body. I traced the profile and used the revolved function to create an new body 
s
![](../projects/Plate/motor2.jpg)

![](../projects/Plate/Motor3.jpg)

Now I used the combined command to cut this out of the base of the plate for a direct mount 


![](../projects/Plate/Motor4.jpg)

Creating a nice mount for the plate - i also think i do not need the spinner base any more. 

![](../projects/Plate/Motor5.jpg)

I knew there was going to be a lot of stress on this when the plate spins so I filet everything I could to strength the joints.

 ![](../projects/Plate/Motor51.jpg)

Got it ready to 3D print 


![](../projects/Plate/Plate3.jpg)




Dan Stone's avatar
Dan Stone committed
## Bowel holder 

Initially I printed a basic arm to get a physical sense of the shape and size 

![](../images/Finalproject/arm11.jpg)

After have a basic shape in the early design I needed to have a pieces that was help in place on the plate. 

I started by adding a wedge at the plate level and tweaking the shape but it was very unstable 

![](../images/Finalproject/arm12.jpg)


I decided to use to features to do that. 

1) Redesign the base to snugly fit on the shape of the plate 


![](../images/Finalproject/arm1.jpg)

![](../images/Finalproject/arm2.jpg)

2) Create a threaded rod on the bottom and print a nut that will hold the are in place 

![](../images/Finalproject/arm3.jpg)


![](../images/Finalproject/arm5.jpg)


![](../images/Finalproject/arm4.jpg)

Dan Stone's avatar
Dan Stone committed
![](../images/Finalproject/arm5.jpg)

![](../images/Finalproject/ARM6.jpg)

Dan Stone's avatar
Dan Stone committed
Here is it assembled 
Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
![](../projects/Plate/holders.jpg)
Dan Stone's avatar
p4  
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
and now to test 
Dan Stone's avatar
p4  
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
<iframe width="560" height="315" src=../../images/Finalproject/Bowlfly.mp4 frameborder="0" allowfullscreen></iframe>  
Dan Stone's avatar
Dan Stone committed


Dan Stone's avatar
Dan Stone committed
## Water skirt and drainage 

My plan for water profing the motor and providing a gravity based drainage is to create a sloped rubber base for box with a rasied skirt. 

The skirt will go between the motor and the plate lip thus stopping any water for getting into the motor. 

I started with a fusion design 

![](../projects/Plate/waterskirt.jpg)

Added the drainage slopes 

![](../projects/Plate/waterskirt2.jpg)

Unfortuntaly my prusa is too small to print the whole things at one so I had to cut it to be printed in parts 

![](../projects/Plate/waterskirt3.jpg)

![](../projects/Plate/waterskirt4.jpg)

Printing in TPU is slow if you do not want stringing It is a 23 hour print !!

![](../projects/Plate/waterskirt5.jpg)

Here it is in progress


![](../projects/Plate/waterskirt6.jpg)

Fully printed

![](../projects/Plate/waterskirt61.jpg)


Printing went well but remove the print from the plate was nearly impossible and ended up destrying the plate. 

This did not happen to me in smaller prints I did but after going back and reviewing the Prusa [materials guide](https://help.prusa3d.com/materials#_ga=2.250429327.883239654.1684193727-1420350994.1684193726) as well as reading some user form it seems that I missed the need to either 
1) Add a layer of glue stick 
2) Put down blue tape the print on 



## Spinning Motor set up 

Dan Stone's avatar
Dan Stone committed
For my vegetable washing machine I initially purchased 3 parts: 

1. 12-24V power supply 

2. 12-24V / 80W DC Motor

3. 12-24V Motor ESC 

![Motor](../images/imagW9/MOT1.jpg)

The ESC is controlled by a Potentiometer and once I got them connected they all worked well together. When 
I turned the knob the motor speed changed. 

I want to be able to control the ESC with the microcontroller so I can adjust the speed for the wash and 
dry cycles. 

First I need to understand how the Potentiometer works with the ESC. There is a plug with power and ground on either side 
the middle wire voltage change based on the potentiometer position ranging from 0.5V to 3.6V.

![Motor](../images/imagW9/MOT2.jpg)

![Motor](../images/imagW9/MOT3.jpg)


I was not sure how to approach this, my initial plan was to use 2 resistors and some relays to switch between 
2 speeds. After reviewing Dr. Gershenfeld class and reflecting on the transistor discussion I came up with the 
idea of used a transistor to replace the potentiometer and a capacitor to smooth out the control signal from the
microcontroller. 

I ran this by our local instructor Mr. Dubick  and my classmate Adam Durrett that have strong electronics background and they 
agreed it should work!!!



## Motor control circuit  design

I decided the set up the board to control both the motor the spin the Vesgtable Basket as well as the Water pump even 
though my focus this week was on the motor. 

For each I would have a control signal come in from the micro controller on the main board. I would change the frequency of 
the signal the change the speed, putting a capacitor on the line would smooth it and would replace the line in with the 
potentiometer.

![Circuit](../images/imagW9/PCB1.jpg)

Not to get things a bit more organized. It is a relatively simple circuit 

![Circuit](../images/imagW9/PCB2.jpg)

Not pushed it to the 2B Board and started tracing 

![Circuit](../images/imagW9/PCB3.jpg)


## Motor control PCB design 

Pushed to the 3D board get ready to mill

![Circuit](../images/imagW9/PCB4.jpg)

![Circuit](../images/imagW9/PCB5.jpg)

When I reviewing the milling it was very tight due to the tracing. 

![Circuit](../images/imagW9/PCB8.jpg)

![Circuit](../images/imagW9/PCB6.jpg)

![Circuit](../images/imagW9/PCB81.jpg)

I reviewed the connectors and saw that by switch a few things around I could simplify the tracing 
and provide more space between traces to make for easier milling 

![Circuit](../images/imagW9/pcb7.jpg)

![Circuit](../images/imagW9/PCB82.jpg)



## Motor control board milling 

Now I was ready to mill. I used the same set up with my Genmitsu 3020-Pro-Max from last week [here](https://fabacademy.org/2023/labs/charlotte/students/dan-stone/assignments/week09/#tool-path-set-up)

The tool path looked good 

![Mill](../images/imagW9/Mill1.jpg)

Got to cutting using a 0.8mm end mill 

![Mill](../images/imagW9/Mill2.jpg)

![Mill](../images/imagW9/Mill21.jpg)

I deburred and washed the board 

![Mill](../images/imagW9/Mill3.jpg)

Now we are ready to stuff and solder 

![Mill](../images/imagW9/Mill4.jpg)

Here are all the components 

![Mill](../images/imagW9/Mill5.jpg)

And we are ready to test 

![Mill](../images/imagW9/Mill6.jpg)

After stripping the connectors  on a number of boards and after rethinking the machine design I decided the break this board into 
2 one for the motor and one for the pump. 

I also increased the side of my traces to 30mil and replace the pad for my connector with A better connector from 
the fab library 

I started testing the board and it seemed like now matter what I did the Sources and Drain of the transistor was always connected. 

I checked for shorts, I added a pull down resistor to ensure the gate is 0 and not joy. The source and drain are connected. 

I went back to the lab and got another 2 transisotr (the lab only had 3 of them) and they all seemed to do that same. 

I reviewed them with my instructure and fellow student who is an electrical engineer and they could not find why it was 
acting this way other then it may be a bad batch of transistors. We put in an order for some more and for now this part 
of the project is on hold until the arrive. 
Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
While this effort was on hold we completed Machine Building week and that changed my mind on how to set up the motor. 
Dan Stone's avatar
Dan Stone committed

## Moving to direct drive

Dan Stone's avatar
Dan Stone committed
After a success full machine week I got appreciation for the out runner motor capabilities and so I decided to try and mount the plat directly on a out runner motor and see if that work. 
Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
I had a outrunner motor in the lab that was bigger then the one we used in machine week and I think would work well.

Here is it spec:

![](../images/Finalproject/motorspec.jpg)

I coupled that with a large ESC with the following [user manual](https://www.rcelectricparts.com/classic-esc-user-guide.html#03)


I decided to test the motor using a potentiometer to control the speed so I can find out what are good speeds for my final project. 

I set up the mounting bracket on the motor 

![](../images/Finalproject/motor1.jpg)

I used a scrap piece of wood to mount the motor onto the frame

![](../images/Finalproject/motor2.jpg)

## ESC wiring 

Power: The motor will connect directly to the 0-24V power supply I have 

![](../images/Finalproject/motor3.jpg)

ESC control: the ESC will be connect to the BOD via 3 wires: 5V / GND / and PMW from pin 9 


## Arduino code for potentiometer control 

I wired a potentiometer to analog input A1 and the 5V/GND and ran the following code: 

```c
# include <Servo.h>

// create a Servo object to control the ESC
Servo esc;

int potVal;

void setup() {
  // set the baud rate for serial communication
  Serial.begin(9600);

  // attach the ESC to pin 9
   esc.attach(9, 1000, 2000); // the second and third parameters are the minimum and maximum pulse widths
  int potVal;
 esc.write(0); //arm ESP
 delay(1000);
}

void loop() {
  // set the speed to half of the maximum (which is 180)
  
 potVal = analogRead(A1); // read input from potentiometer.

int speed  = map(potVal,0, 1023, 0, 180); // maps potentiometer values to PWM val

  // send the speed to the ESC
  esc.write(speed);

   // print the speed to the serial monitor
  Serial.print("Speed: ");
  Serial.println(speed);
 
  // pause for a moment before starting again
}
```

This will both printout in the serial monitor the speed variable so I can see the which value I would want to use in the final code. 

## First time ESC calibration 

When you plug the ESC in for the first time it need to go via a calibration process. 
1) You put it to full throttle  
2) Connect motor to power 
3) Move to zero throttle

You can see the motor first run 

<iframe width="560" height="315" src=../../images/Finalproject/ESCcalib.mp4 frameborder="0" allowfullscreen></iframe>  


## Motor speed test 

I mounted the plate on the motor and ran the motor

Dan Stone's avatar
Dan Stone committed
<iframe width="560" height="315" src=../../images/Finalproject/spiningplate.mp4 frameborder="0" allowfullscreen></iframe>  

Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
I started moving the potentiometer while look at the serial monitor to see the speed. 
Dan Stone's avatar
Dan Stone committed

Dan Stone's avatar
Dan Stone committed
<iframe width="560" height="315" src=../../images/Finalproject/speed.mp4 frameborder="0" allowfullscreen></iframe>  

Dan Stone's avatar
Dan Stone committed
Answer is pretty straight forward. 

The lowest speed that will run is with the Servo Angle value of 24. 

A good increased speed for drying is 40. 

These will be the two value I will use in the cycles





Dan Stone's avatar
Dan Stone committed


Dan Stone's avatar
Dan Stone committed
## Code basic set up 

To keep this week in sync with my final project I decided to test a set up for the basic VMS functionality 
replacing the water pump and motor with LED and the sensors with buttons. 

Here is the functionality I was aiming for:



|  Button |  Label | FUnctionality  |
|---|---|---|
| Button 1  | Wash cycle  |   1. Check Lid / Water sensor -> 2. Turn on Water pump and motor for a set time | 
| Button 2  | Dry cycle  |  1. Check Lid -> 2. Turn on motor for a set time |   
|  Button 3 |   Total cycle |  1. Run Wash cycle -> 2. Run Dry cycle | 
|  Sensors |  If either sensor is triggered then stop and turn on error LED |   | 

Here is my updated code:

```c
// Define the pin numbers for the sensors and actuators
const int LED_PIN = 7;
const int WASH_BUTTON_PIN = 11;
const int DRY_BUTTON_PIN = 10;
const int FULL_BUTTON_PIN = 9;
const int WATER_SENSOR_PIN = 2;
const int LID_SENSOR_PIN = 3;
const int DRUM_PIN = 4;
const int WATER_PUMP_PIN = 5;

void setup() {
    Serial.begin(9600);
    pinMode(LED_PIN, OUTPUT);
    pinMode(WASH_BUTTON_PIN, INPUT);
    pinMode(DRY_BUTTON_PIN, INPUT);
    pinMode(FULL_BUTTON_PIN, INPUT);
    pinMode(WATER_SENSOR_PIN, INPUT);
    pinMode(LID_SENSOR_PIN, INPUT);
    pinMode(DRUM_PIN, OUTPUT);
    pinMode(WATER_PUMP_PIN, OUTPUT);
}

void loop() {
    // Wait for the wash button press
    if (digitalRead(WASH_BUTTON_PIN) == HIGH) {
        // Check the water level and lid status
        if (digitalRead(WATER_SENSOR_PIN) == LOW && digitalRead(LID_SENSOR_PIN) == LOW) {
            // Start the wash cycle
            digitalWrite(DRUM_PIN, HIGH);
            digitalWrite(WATER_PUMP_PIN, HIGH);
            delay(600);
            digitalWrite(DRUM_PIN, LOW);
            digitalWrite(WATER_PUMP_PIN, LOW);
              delay(400);
              digitalWrite(WATER_PUMP_PIN, HIGH);
           delay(400);
            digitalWrite(WATER_PUMP_PIN, LOW);
        } else {
            Serial.println("Not enough water or lid is open.");
                        digitalWrite(LED_PIN, HIGH);

        }
    }

    // Wait for the dry button press
    if (digitalRead(DRY_BUTTON_PIN) == HIGH) {
        // Start the slow spin
                if (digitalRead(LID_SENSOR_PIN) == LOW) {

        digitalWrite(DRUM_PIN, HIGH);
        delay(600);

        // Start the fast spin
        digitalWrite(DRUM_PIN, LOW);
        delay(300);
        digitalWrite(DRUM_PIN, HIGH);
        delay(300);
        digitalWrite(DRUM_PIN, LOW);
                }     else {
            Serial.println("lid is open.");
                        digitalWrite(LED_PIN, HIGH);

        }
    }

    // Wait for the full cycle button press
    if (digitalRead(FULL_BUTTON_PIN) == HIGH) {
        // Perform the wash cycle
        if (digitalRead(WATER_SENSOR_PIN) == LOW && digitalRead(LID_SENSOR_PIN) == LOW) {
            // Start the wash cycle
            digitalWrite(DRUM_PIN, HIGH);
            digitalWrite(WATER_PUMP_PIN, HIGH);
            delay(600);
            digitalWrite(DRUM_PIN, LOW);
            digitalWrite(WATER_PUMP_PIN, LOW);
                delay(400);
            digitalWrite(WATER_PUMP_PIN, HIGH);
           delay(400);
            digitalWrite(WATER_PUMP_PIN, LOW);
        } else {
            Serial.println("Not enough water or lid is open.");
             digitalWrite(LED_PIN, HIGH);
            return;
        }

        // Perform the dry cycle
        // Start the slow spin
        if (digitalRead(LID_SENSOR_PIN) == LOW) {
        digitalWrite(DRUM_PIN, HIGH);
        delay(200);

        // Start the fast spin
        digitalWrite(DRUM_PIN, HIGH);
        delay(200);
        digitalWrite(DRUM_PIN, LOW);
        delay(200);
        digitalWrite(DRUM_PIN, HIGH);
        delay(100);
        digitalWrite(DRUM_PIN, LOW);
    
       } else {
            Serial.println("Not enough water or lid is open.");
             digitalWrite(LED_PIN, HIGH);
            return;
        }

    }}
```


Here is the basic circuit I am planning 

![Circuit](../images/ImagW4/Arduino1circuit.jpg)


I followed this diagram (except for the different colored wires) and it went pretty smoothly

Here is the one I built in action:

<iframe width="560" height="315" src="https://www.youtube.com/embed/PIB-q0JtLqo" title="YouTube video player" frameborder="0" allow="accelerometer; autoplay; clipboard-write; encrypted-media; gyroscope; picture-in-picture; web-share" allowfullscreen></iframe>


## New board - Moving to RO2040

After a while I decided to move to a working iwht th eRP2040 

I am going to follow the same break out board design and so I started to work on a schematic. I am planning to use 
4 pin wire to board connectors and 2 pin for the power as an alternative to the USBC.

![](../projects/Board/Newboard1.jpg)

I have the 2D Board set up 

![](../projects/Board/Newboard2.jpg)

Now we are ready to mill 

![](../projects/Board/Newboard3.jpg)

Here we are in action 

![](../projects/Board/Newboard4.jpg)



![](../projects/Board/Newboard5.jpg)


![](../projects/Board/Newboard61.jpg)


![](../projects/Board/Newboard6.jpg)


![](../projects/Board/Newboard62.jpg)


![](../projects/Board/Newboard63.jpg)


![](../projects/Board/Newboard64.jpg)


![](../projects/Board/Newboard65.jpg)


![](../projects/Board/Newboard66.jpg)


![](../projects/Board/Newboard7.jpg)


![](../projects/Board/Newboard71.jpg)
Dan Stone's avatar
Dan Stone committed

I used this board in a number of weeks but decided to redo it so it has a shape of a vegetable 

## Button board 

To connected the control button, lid sensor and water level sensor I created a break out board. 

I started with a basic schematic 

![](../images/Finalproject/BB1.jpg)

I think routed the board and decided to make the board the shape of a carrot. 

![](../images/Finalproject/BB2.jpg)

I had to shorten the carrot so it fit on the PCB I had.

![](../images/Finalproject/BB3.jpg)

And now it is ready to mill 

![](../images/Finalproject/BB4.jpg)

Here we go 

![](../images/Finalproject/BB5.jpg)

No we just have to clean it up 

![](../images/Finalproject/BB6.jpg)
Dan Stone's avatar
Dan Stone committed


I got that parts soldered in and set up with the motor. 



## Button turning motor 


I soldred the wire for the button as well as the 4 pin connector to the button board 


 ....


## Pump breakout board 

I initialy toughts this should be pretty traight forward. 

Breakout board would drive a relay with a GPIO from the main board that would be activated but the button push similar to the motor. The relay would connect the pump to the 12V power supply. 

![](../projects/pumpboard/P1.jpg)

I decided to use a mushroom design 

![](../projects/pumpboard/P2.jpg)

got it ready to cut 

![](../projects/pumpboard/P3.jpg)

![](../projects/pumpboard/P4.jpg)


I misjudged the size and so after overshotting 

![](../projects/pumpboard/P61.jpg)

I redesigned the board 

![](../projects/pumpboard/P5.jpg)


![](../projects/pumpboard/P6.jpg)

Got it cut 

![](../projects/pumpboard/P7.jpg)

Not it fit 

![](../projects/pumpboard/P71.jpg)

Got it stuffed and soldered 

![](../projects/pumpboard/P72.jpg)



When I pressed the button the motor turned byut instead of the rely switching to turn on the pump nothing happened.

I got out the multimeter and saw that when not connected to the relay the D1 pin  went up to 3.3V when I pressed the button but when connected to the relay it only went to 1.8V and the relay did not activate. 
 
I researched this I found out the RP2040 GPIO do not have enough current to drive  the relay so I needed to make a driver.

I found this basic driver schematic on the [raspberrypi forum](https://forums.raspberrypi.com//viewtopic.php?t=63578&p=470362#p470625)

![](../projects/pumpboard/Relaydriver1.jpg)

I only had through hole components to make this and so decided to make a through hole board for this. I never made one and so was interested to see how it worked.  

First I tested it on a breadboard to make sure it worked 

![](../projects/pumpboard/P73.jpg)


Updated the schematic to include the driver. 

![](../projects/pumpboard/P8.jpg)

Retraced everything 

![](../projects/pumpboard/P81.jpg)

Got it ready to mill 

![](../projects/pumpboard/P82.jpg)